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49

ELECTRONIC DEVICE FAILURE ANALYSIS | VOLUME 18 NO. 2

After 10 to 30 s, the acid is rinsed with acetone for neu-

tralization. The process is repeated until the die and wire

bonds of the package are exposed.

While the rotary-tool method is the standard practice,

it does have some drawbacks:

• The drilling process introduces an outside source of

disruption to the device.

• The drilled well still allows the nitric acid to flow from

the surface of the encapsulant.

• It is difficult to direct where the acid is working on the

encapsulant.

THE SOLUTION

Faced with the shortcomings of the current process,

the company set out to find a better solution. They dis-

covered that Texas Instruments had successfully used

a 2078 Viton Caulk from Pelseal Technologies to assist

with decapsulation. This caulk exhibits strong chemical

properties and remains flexible in service. The company

decided to adopt this approach by using the caulk to build

up awell to contain the nitric acid, rather than drilling into

the component.

[1]

To form the well, ACI built up approximately 2 to 4 g

of caulk above the die location (in place of carving out a

small well) and placed the component on the hot plate.

When the component reached the correct temperature,

the operator droppednitric acid into the fabricatedwell to

allow digestion of the packaging material. This was then

rinsed with acetone, and the process was repeated until

the die was exposed.

After using the caulk-constructed well method of

decapsulation, the company found:

• By not drilling directly into the surface of the die, no

additional mechanical damage was introduced.

• Electrostatic discharge/electrical overstress was

removed from the equation, thus increasing the con-

fidence in the results.

• The caulk adheres easily to awide range of component

materials.

• The caulk was easily removed after decapsulation by

simply tugging on it with a pair of tweezers. (The caulk

stood up to repeated acetone rinse steps.)

• The depositionof the caulk permits outlining of various

geometries, making it possible to use it with a wide

range of die sizes and shapes.

• Safety is increased by creating a well on the surface

of the die that stands above the original topography,

eliminating any splashing or accidental misuse of

concentrated acids.

• A larger quantity of acid could be used in the caulk-

constructed well, resulting in less time needed for the

decapsulation process.

After determining that the use of a caulk well made

the decapsulation process easier and more effective, the

engineering research company decided to continue using

the caulk, and they plan to integrate it into their standard

decapsulation procedures.

REFERENCE

1. K.D. Staller: “Safe Decapsulation Techniques Using Viton Caulk,”

Proc. 40th Int. Symp. Test. Fail. Anal. (ISTFA 2014),

Nov. 9–13, 2014

(Houston, Texas).

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